Before taking part in the Cleaner
Production Component, due to poor equipment, the company had to face
many environmental problems such as toxic exhausted fumes from furnace
and material dryer system and a large amount of dusts eliminated to the
environment.
To produce one tonne of cement, the material dryer
system emits 13kg of wastes, with the stage of grinding and transporting
material eliminating 5kg of stone dust, furnaces 10kg of dusts and
exhausted fumes, material metering stage 1.5kg of clinker dusts and
packing stage 1.5kg of cement. Wastes that contain a large amount of
materials cause wastage and the environmental pollution.
Aware of
the situation, the Luu Xa Cement Factory has focused on application of
cleaner production methods. In 2002, the first methods were proposed.
Due to lack of experiences in this field, the factory did not obtained
many remarkable achievements. In 2007, receiving supports from the
Ministry of Industry and Trade and the Vietnam Cleaner Production
Center, the factory took part in the Cleaner Production Component. Since
then, a number of cleaner production methods have been applied. For
example, the company emitted a large amount of dusts to the environment.
There are many reasons for this situation. The covers that prevent
materials and cement from leaking out are torn. Workers' skill is not
high. In addition, clinker is poured on the ground, and then scooped up
on vans. Thus, they wasted a large amount of materials. Some methods
were applied to solve this wastage. Torn covers have been replaced or
repaired. Clinker is poured directly to vans. Wasted materials are
withdrawn. Thanks to these methods, dusts emitted to the environment are
remarkably reduced.
Before taking part in the Cleaner Production
Component, the factory often had technical problems, so furnaces often
had to stop running suddenly. Workers were not aware of energy saving,
so they often let machines run idle. Energy conservation lighting system
was not used. Therefore the factory consumed a huge amount of
electricity. Many methods to reduce electricity consumption were
applied. Inverters have been installed for suitable conveyor belts.
Compact lamps have been used. In addition, the factory has focused on
improving workers' awareness of energy conservation. These methods cost
VND245 million. With these methods, the factory saves VND390 million on
electricity annually.
In terms of coal consumption, the factory
wasted 45 tonnes of coal because workers did not know how to run furnace
properly. They provided too much or too dry coal for furnaces and often
opened furnace doors. Therefore, the factory has applied some methods
like using suitable amount of coal with proper moisture to burn furnaces
and avoiding opening furnace doors. Thanks to these methods, the
factory saves VND40 million spent on coal annually.
Following
success of simple methods, the factory has invested in methods that
require large capital. For example, the factory knows that the open jaw
crusher system and the lack of dust collector are the main reasons for a
large amount of dust emitted to the environment. Therefore, the open
jaw crusher system has been replaced with closed system and a dust
collector has been installed. Thanks to the new system, the amount of
dust in the air has been decreased. Dusts are withdrawn and recycled.
The new system which costs VND1.3 billion helps the factory save VND27.6
million annually. In addition, the factory’s exhausted fumes meet the
TCVN5939:2005 standard.
In addition, before taking part in the
Cleaner Production Component, the factory used old material dryer system
that produced low capacity. Some methods to raise the material dryer
capacity have been applied. An automated temperature controller of the
air supplied for the dryer system has been applied. The dryer system has
been improved to raise heat exchange capacity. Gas pipe and dryers have
been covered with a heat isolating layer to reduce heat leaking out. A
dust collector has been installed. These methods cost VND1.513 billion.
Every year, the factory saves VND167.4 million thanks to recycling
withdrawn materials. In addition, these methods help the company reduce
48 tonnes of dusts eliminated to the environment and 55,000cu.m of water
annually.
Thanks to effective energy conservation methods, the
Luu Xa Cement Factory has become one of typical businesses in the field
of cleaner production in Thai Nguyen Province./.
By Bao Ngoc